LewanSoul LDX-227 Digital Robot Servo (movement issue)

Mechanics Getting Coffee
Mechanics Getting Coffee
3.3 هزار بار بازدید - 6 سال پیش - Testing the LewanSoul LDX-227 Digital
Testing the LewanSoul LDX-227 Digital Robot Servo with the following setup:

= Arduino UNO R3 board
= 7.4 V, 1.5 A bench power supply
= Servo hooked up to Pin 4 (digital output pin) of the Arduino UNO R3 board
= A square wave with a pulse period of 20ms is implemented in the Arduino IDE source code

Issue: the movement of the servo is very jerky and does not provide the expected smooth movement despite setting up the test according to the servo's requirements

If you have any ideas or suggestions on how this can be resolved, please don't hesitate to comment and let me know below, thank you!
6 سال پیش در تاریخ 1397/03/31 منتشر شده است.
3,332 بـار بازدید شده
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